热电厂烟气余热回收技术在能源结构调整中的应用研究

Application of flue gas waste heat recovery technology in energy structure adjustment of thermal power plants

  • 摘要: 针对热电厂高温烟气直接排放造成的能源浪费与环境污染问题,结合某300MW燃煤热电厂典型案例,构建了一套集喷淋冷却、直接接触式换热、热源热泵与燃气锅炉多级耦合的烟气余热回收系统。通过对烟气显热与潜热的分段提取与有效利用,实现了余热向一次供热系统的转化。系统设计包括热能分析模型建立、换热模块配置、输送利用策略及智能监控机制制定,并在不干扰主系统运行的前提下完成工程部署。运行数据显示,改造后烟气排放温度降至约30°C,热效率提升至80%以上,年节煤量达4万t,CO2与NOx排放量显著下降。本研究为热电行业能源结构优化与供热系统绿色转型提供了可推广的技术示范。

     

    Abstract: To mitigate energy loss and emissions from high-temperature flue gas in thermal power plants, this study develops a multi-stage recovery system for a 300MW coal-fired unit. Integrating spray cooling, direct contact exchangers, heat pumps, and gas boilers, the system efficiently recovers sensible and latent heat for district heating. Without disrupting main operations, the retrofit lowers flue gas temperature to 30°C, boosts efficiency above 80%, and cuts annual coal use by 40,000 tons, offering a replicable path for green energy transition in the thermal power industry.

     

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